1st build guidance needed:
Advance apologies.
1st tubes out turn on went well. Realized my ExTech multimeter wasn't up to the task. Hubris had me do a tubes-in test before getting a meter up to the task.
As soon as standby turned off I heard the cab make a rippling sound and was thinking //is this the "motorboating" everyone talks about when OT leads are backwards?//
I tried to switch between Tube and S.S. rectification in my blind-man's search to isolate the issue. No real change.
After about 3 minutes I saw a tendril of smoke from the area of the presence knob and as I was looking to see which component was dying there was a percussive bang and flash.
I turned off amp, let the caps drain a bit and opened the rear.
It was obvious that R36 (1k/3w) was toasted and the nearest 10uF/100V C13 had blown its guts. [YES! - all polarities of caps and diodes were (and are) correct to layout/schematics]
https://el34world.com/Hoffman/files/Hoffman_5F6A.pdfA few things I quickly felt shame for:
1) being an over-confident idiot and not going through proper procedural tests.
2) I had forgotten to reflow R27 220k after making the under-board connection. I had meant to do it before mounting board in chassis to ensure reflow wouldn't affect that connection while it could still be visually verified (see point #1)
So now I have
A) Reflowed R27.
B) Replaced C13 &C14.
C) Replaced R36.
Without a doubt, I will proceed to tubes removed testing and further rechecking for shorts or mistakes.
My 2 questions for the forum are:
1) was bad connection to R27 or the underboard connection to bias responsible for destruction of R36 and C13? R36 was glowing like the sun before C13 exploded. My gut reaction is that something else is amiss.
2) what else could have been damaged beyond the destroyed R36 and C13? Should I worry about the bias pot and diode?
Any and All constructive comments are appreciated.
"But if I do not strive...who will?" - Lao Tzu